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Continuous tannin extraction by use of screw reactor, TAPPI Journal February 2021

ABSTRACT: A pilot-size screw reactor (extraction unit) was used for tannin extraction of spruce. Yield of the same magnitude or better was obtained when comparing a screw reactor with batch reactors. A longer presoaking time in water seemed to be better than a short one for obtaining higher yield. A higher yield is obtained with lower dry-water ratio, which suggests that the internal diffusion in bark does not determine mass transfer as much as is the case without presoaking of bark. The higher dry-water ratio decreased the yield. The prior soaking of the bark also minimized the mechanical reactor feeding problems (clogging). The benefits of a screw reactor likely are that run time changes for different process conditions are flexible; it simplifies design and construction of an industrial unit for tannin production; and it saves space because of the need for fewer and smaller intermediate storage tanks.

Journal articles
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Open Access
Addressing production bottlenecks and brownstock washer optimization via a membrane concentration system, TAPPI Journal July 2021

ABSTRACT: Advancements in membrane systems indicate that they will soon be robust enough to concentrate weak black liquor. To date, the economic impact of membrane systems on brownstock washing in kraft mills has not been studied and is necessary to understand the viability of these emerging systems and their best utilization.This study investigated the savings that a membrane system can generate related to brownstock washing. We found that evaporation costs are the primary barrier for mills seeking to increase wash water usage. Without these additional evaporation costs, we showed that our hypothetical 1000 tons/day bleached and brown pulp mills can achieve annual savings of over $1.0 MM when operating at higher dilution factors and fixed pulp production rate. We then investigated the impact of increasing pulp production on mills limited by their equipment. In washer-limited mill examples, we calculated that membrane systems can reduce the annual operating cost for a 7% production increase by 91%. Similarly, in evaporator-limited mill examples, membrane systems can reduce the annual operating cost for a 7% production increase by 86%. These results indicated that membrane systems make a production increase significantly more feasible for these equipment-limited mills.

Journal articles
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Open Access
New learnings and strategies for meeting future recovery boiler particulate emission limits with existing electrostatic precipitators, TAPPI Journal June 2021

ABSTRACT: It is foreseeable that recovery boiler particulate emission limits in the United States and Canada will continue to get more stringent with time. Because of this, continued improvement of emission control equipment, as well as a better understanding of how operating parameters affect performance, are necessary. Although electrostatic precipitators (ESPs) are often viewed as a mature technology, many improvements in ESP technology continue to be developed. In recent years, academic efforts have improved the understanding of recovery boiler operating conditions on ESP performance. Additionally, advancements in materials, power supplies, and design continue to improve the efficiency and reliability of ESPs.This paper discusses how recovery boiler and electrostatic precipitator (ESP) operating factors affect ESP perfor-mance based on process simulations and practical experience, and how these learnings can be implemented to improve future operation of existing ESPs.

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Open Access
Repulping of wet strength paper towel with potassium monopersulfate, TAPPI Journal September 2020

ABSTRACT: Potassium monopersulfate (KMPS) was used in repulping of polyamide-epichlorohydrin (PAE)-containing paper towel. The effectiveness of the repulping aid was compared with that of sodium hypochlorite. Addition of a 2.4% KMPS repulping aid achieved complete repulping of the paper towel, resulting in 88% screen yield and about 5% rejects. To reach a similar pulping result, two times the oxidative equivalent amount of sodium hypochlorite had to be used. Compared to the pulp fibers obtained from sodium hypochlorite repulping, those obtained from KMPS repulping had higher physical strength, longer fiber length, and lower fines content. This study demonstrated that KMPS was superior to sodium hypochlorite in repulping of PAE-containing paper towel in terms of effectiveness and pulp quality.

Journal articles
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Open Access
Crossflow filtration of green liquor for increased pulp production, improved green liquor quality, and energy savings, TAPPI JOURNAL October 2020

ABSTRACT: A new green liquor filtration system has been installed and commissioned at the Ence pulp mill in Pontevedra, Spain. The filtration system is based on microfiltration and was developed in collaboration with the KTH Royal Institute of Technology in Stockholm, Sweden. The patented method for efficient purification of green liquor decreases the non-process element (NPE) content by providing more efficient solids/liquid separation, reducing energy and chemical consumption in pulp mills and increasing production capacity by eliminating certain capacity bottlenecks. The process has been continuously tested at the Aspa Bruk Mill outside Askersund, Sweden, since 2013. The technology has proven to create nearly particulate-free green liquor during the purification process. The technology can also be used to polish white liquor to provide higher pulp quality.To provide for a simple and cost-effective installation, the system was designed as a skid-mounted unit that is pre-piped, instrumented, and tested before shipment. The system is modular and allows for easy expansion of capacity. This paper discusses the process design, process integration, and startup of the new system, along with experiences from the first months of operation.

Journal articles
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Open Access
Optimizing OCC refining with defloccing, TAPPI Journal April 2025

ABSTRACT: Subjecting pulp to a high shear zone immediately after refining results in more efficient refining. This phenomenon was originally observed to benefit softwood pulp refining. It was attributed to floc reduction based on floc measurements in mill refiners and the observation of reduced headbox plugging. Hence, this phenomenon has been termed “defloccing.” The present work shows this technology also benefits refining of North American old corrugated containers (OCC). The combined results of several mill trials with OCC defloccing demonstrate the interactions between OCC refining intensity, defloccing technology, and other state-of-the-art refining improvements. At the same refining intensity, defloccing OCC on 100% recycled machines increases OCC refining efficiency by 15%, with greater efficiency improvement on machines that use softwood as well as OCC. Furthermore, it is shown that the benefits of defloccing are additive to refining improvements made in the refining zone of a refiner plate. Most OCC refiner plate designs can therefore benefit from the addition of a defloccing feature.

Journal articles
Open Access
Gap mechanics in pulp refiners, TAPPI Journal June 2025

ABSTRACT: Studies of pulp refining have shown that a single bar impact on pulp has only a 1%•5% probability of producing a successful refining effect. This study has explored the reason why. An analysis of refining kinetics suggested that small segments of a fiber length, about a fiber diameter in size, are treated during each impact. Measurements of localized swelling along fiber lengths caused by refining supported this finding. Based on these findings, it was postulated that force transmittal through fiber networks occurred primarily at fiber crossings. The small size of fiber diameters relative to fiber lengths accounts for the low probability of a successful refining event at each impact. This probability, and the probability of fibers being captured and impacted during passage through a refiner, account for the need for multiple bar crossings to refine pulps.

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Open Access
Boiler retrofit improves efficiency and increases biomass firing rates, TAPPI Journal March 2021

ABSTRACT: Domtar’s fluff pulp mill in Plymouth, NC, USA, operates two biomass/hog fuel fired boilers (HFBs). For energy consolidation and reliability improvement, Domtar wanted to decommission the No. 1 HFB and refurbish/retrofit the No. 2 HFB. The No. 2 HFB was designed to burn pulverized coal and/or biomass on a traveling grate. The steaming capacity was 500,000 lb/h from coal and 400,000 lb/h from biomass. However, it had never sustained this design biomass steaming rate. As the sole power boiler, the No. 2 HFB would need to sustain 400,000 lb/h of biomass steam during peak loads. An extensive evaluation by a combustion and boiler technologies supplier was undertaken. The evaluation involved field testing, analysis, and computational fluid dynamics (CFD) modeling, and it identified several bottle-necks and deficiencies to achieving the No. 2 HFB’s biomass steam goal. These bottlenecks included an inadequate combustion system; insufficient heat capture; excessive combustion air temperature; inadequate sweetwater con-denser (SWC) capacity; and limited induced draft fan capacity.To address the identified deficiencies, various upgrades were engineered and implemented. These upgrades included modern pneumatic fuel distributors; a modern sidewall, interlaced overfire air (OFA) system; a new, larger economizer; modified feedwater piping to increase SWC capacity; replacement of the scrubber with a dry electrostatic precipitator; and upgraded boiler controls.With the deployment of these upgrades, the No. 2 HFB achieved the targeted biomass steaming rate of 400,000 lb/h, along with lowered stack gas and combustion air temperatures. All mandated emissions limit tests at 500,000 lb/h of steam with 400,000 lb/h of biomass steam were passed, and Domtar reports a 10% reduction in fuel firing rates, which represents significant fuel savings. In addition, the mill was able to decommission the No. 1 HFB, which has substantially lowered operating and maintenance costs.

Journal articles
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Open Access
Peracetate/singlet oxygen chemistry used in post-bleaching of kraft pulp as a practical oxidant for paper machines, TAPPI Journal May 2021

ABSTRACT: The use of a novel sodium peracetate/singlet oxygen chemistry for brightening bleached kraft pulp shows exciting potential for technical performance, supply logistics, safety, and cost reduction. Potential chemical carryover to the paper machine raises questions about whether peracetate will impact paper machine performance, such as metal corrosion, useful press felt life, and interference with existing biocide programs or paper machine chemistry. Sodium peracetate/singlet oxygen chemistry can be used in high-density storage chests for brightening/whitening and to increase color stability. Any oxidant used directly before the paper machine has the possibility of impacting paper machine operations. Traditional oxidants used in bleaching, such as chlorine dioxide and hydrogen peroxide, are known to cause corrosion on machinery metals and press felts. Hydrogen peroxide residuals can interfere with common biocide programs. Traditional oxidants used in biocide treatments themselves significantly degrade press felt life when the rule-of-thumb concentration thresholds are exceeded. Sodium peracetate is evaluated in this paper for its impact on nylon press felt fiber degradation, metal corrosion, and interference with typical biocide programs.Laboratory results indicate that sodium peracetate/singlet oxygen chemistry is less corrosive than chlorine, bromine, and hydrogen peroxide on press felt nylon fiber and can therefore be used at higher levels than those chemistries to increase brightness without increasing negative downstream impact. Sodium peracetate can also be used with current biocide programs without negative impacts such as consumptive degradation. Higher residuals of peracetate going to the paper machine may be useful as a biocide itself and can complement existing programs, allowing those programs to stay within their safe operating levels and thereby extend press felt useful life.

Journal articles
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Open Access
Gas dispersion in the oxygen delignification process, TAPPI Journal May 2021

ABSTRACT: There has been very little knowledge about the state of gas dispersion in the oxygen delignification process, even though this has a major impact on the performance of the reactor. This paper presents a new continu-ous inline method for measuring oxygen bubble size distribution in the reactor, as well as results from studies con-ducted in softwood and hardwood lines. This new measurement worked well, and new information about oxygen bubble size, as well as how different reactor conditions affected the distribution, was obtained. For example:œ In the softwood line, the mean volume-weighted bubble size was about 0.1 mm, whereas in the hardwood line, this size was almost 10 times higher. For both lines, there was considerable variation in the measured bubble size over the long term.œ For both lines, an increase in mixer rotation speed caused a discernible decrease in the bubble size, and an increase in oxygen charge caused a discernible increase in the bubble size.œ In the softwood line, no coalescence of the bubbles in the reactor was observed, but in the hardwood line, some coalescence of the larger bubbles occurred.œ In the test conducted in the hardwood line, the use of brownstock washer defoamer caused a discernible increase in oxygen bubble size.œ In the hardwood line, reactor pressure had a noticeable effect on the amount of delignification, which indicated that improving mass transfer of oxygen (e.g., by decreasing the oxygen bubble size, in this case) should also have an increasing effect on the delignification.